2RTsGV
New member
Had my recall work completed yesterday @ Pitbull Powersports in Springfield.
(Many thanks to Len and his crew for tackling this job for me)
Trip home to Kansas City today (250 miles) via Purdy Mo at 72 mph on highways 44 & 49, took about 4.5 hours (stopped for lunch in Lamar Mo) Temps ranged between 80 to 87.
My thoughts on the fix:
Pros:
- Personally I like the look of the scoops
- did not notice any additional engine noise
- Tupperware on right side no longer gets hot
- No heat coming up through the seat area & glove box contents stay cool
- Topped off gas twice (both times with over 100 miles on the existing tank) and no sign of boiling gas, plus the neck of the filler is no longer too hot to touch!
- No gas fumes!
- Bike seemed to perform better
- Temp gauge did not get hotter than halfway
Cons: (though not really a con)
- seems more hot air is coming up from beneath the right side foot area however the heat is about 50% less than it has been in the past
(Many thanks to Len and his crew for tackling this job for me)
Trip home to Kansas City today (250 miles) via Purdy Mo at 72 mph on highways 44 & 49, took about 4.5 hours (stopped for lunch in Lamar Mo) Temps ranged between 80 to 87.
My thoughts on the fix:
Pros:
- Personally I like the look of the scoops
- did not notice any additional engine noise
- Tupperware on right side no longer gets hot
- No heat coming up through the seat area & glove box contents stay cool
- Topped off gas twice (both times with over 100 miles on the existing tank) and no sign of boiling gas, plus the neck of the filler is no longer too hot to touch!
- No gas fumes!
- Bike seemed to perform better
- Temp gauge did not get hotter than halfway
Cons: (though not really a con)
- seems more hot air is coming up from beneath the right side foot area however the heat is about 50% less than it has been in the past